Case Study 6: Pollution Prevention Beyond Regulated Materials
The most successful pollution prevention programs involve looking for
opportunities "beyond the barrels." While pollution prevention most
commonly takes the form of chemical use and waste reduction, by maintaining
a chemical-specific focus you may overlook less obvious opportunities,
such as in energy and water conservation. For one facility, Tri-Star
Technologies, Inc. in Methuen, Massachusetts, broadening their view
of pollution prevention led them to energy and water use reductions
that have resulted in significant cost savings. These energy and water
reduction projects are the focus of this case study.
- CO2 (global warming) of 212,100 pounds;
- SO2 (acid rain) of 1,700 pounds; and
- NOx (acid rain & smog) of 600 pounds.
- CO2 (global warming) of 181,300 pounds;
- SO2 (acid rain) of 1,500 pounds; and
- NOx (acid rain & smog) of 500 pounds.
- conserves water;
- does not use solvents; and
- does not use any chemicals.
Tri-Star Technologies, Inc. is a manufacturer of double-sided and multilayer printed wiring boards, specializing in products for the electronics industry. With 220 employees at their 120,000 ft2 facility, they produce 1,000,000 surface square feet annually.
As Tri-Star implemented their pollution prevention program, this company discovered that demonstrating cost savings is the key to a successful pollution prevention program, especially when first getting started or when jump starting a slow-moving program. Initially, Tri-Star implemented a few projects that did not require much, if any, capital investment. When it was able to show that cost savings achieved from these projects, the credibility of pollution prevention as a good business practice grew.
Today, with several successes to their credit (both from an economic and a waste reduction standpoint), Tri-Star's pollution prevention team is able to obtain funding for projects that do require larger capital investments. These projects also offer increased cost savings in the long term. For example, the facility is currently installing a cupric chloride regeneration system to recycle their inner-layer etchant (see DfE Printed Wiring Board Case Study 2 for more information on etchant regeneration). Such a system might require a capital investment of $150,000 or more, but the payback is expected to be less than 18 months through dramatic reductions in spent (hazardous) etchant and virgin chemical purchases, and by selling the recovered copper by-product. Requiring a significant investment, this project has come about only after the pollution prevention concept gained credibility through the success of "low tech/no tech" projects.
By looking beyond regulated materials, Tri-Star found cost saving opportunities in energy and water conservation. Such opportunities are a "cheap, easy, and often overlooked way to reduce your facility's environmental impact while saving money," says Ed Gomes, environmental Health and Safety Manager for the facility. Energy reductions can lead to reductions in the by-products of energy use that cause global warming, acid rain, and smog -- this is pollution prevention on a global scale. While not all of their projects are directly transferable to every facility, other manufacturers could use the information gained from Tri-Star's experience to examine their own energy and water use.
Utilizing the Utilities
Tri-Star has implemented several energy conservation projects. The two projects described in this case study both involved collaborative efforts with the electric and/or gas companies. Together, these two projects have resulted in savings of thousands dollars per month, or about $51,800 annually.
Tri-Star's first energy conservation opportunity was identified in their fixed flow-rate air make-up units. The facility has several pieces of equipment exhausting air, including wet scrubbers and an electrostatic precipitator. To balance the air flow, they had been using two gas-fired air make-up units, each with a capacity of 40,000 cubic feet per minute (cpm). Since these operated at a fixed rate, they were on continuously, even during non-production hours.
In addition to the operating energy they consumed, the units also required the air conditioning or heating systems to work overtime. In the summer, the units blew hot, humid air into the facility. In the winter, the units heated the air blown in. This resulted in a concentrated heat source that caused great temperature inconsistencies throughout the building, with the hot air in some areas shutting down the thermostats, making the cold areas even colder.
Working with the gas and electric companies, Tri-Star found state-of-the-art variable speed controllers that could be retrofitted to the make-up air units. With the variable speed controllers, the flow rate is determined based on the air exhaust rate from the exhausting equipment. Significant savings in electric and gas bills were realized. A unique feature of this project is that it required no capital investment; the electric and gas company paid for the new equipment.
The facility estimates annual savings to be $22,900 on gas and $15,600 on electricity. Additionally, the project reduced air pollution through energy savings of 31,000 therms and 192,800 kilowatt-hours (KWH). This translates to annual reductions of:
In another energy conservation project, Tri-Star examined their compressed air situation. They had been using two 100 HP and two 50 HP compressors to provide the facility with compressed air. These units had some trouble meeting the compressed air demand. With help from the "Energy Initiative" program run by the electric company (Mass Electric) and input from a consultant, the facility investigated its compressor situation. Based on the results of theresults Tri-Star:
a reserve air tank
replaced the four compressors of 300 HP combined capacity with three
50 HP energy efficient compressors (150 HP combined capacity)
set up the units to cycle based on the compressed air demand in the facility
These changes have saved energy and eliminated the problems in meeting the facility demand for compressed air. Annual energy cost savings from this project are estimated to be $13,300, based on a 164,800 KWH reduction in electricity use. This translates to annual reductions of:
Conserving Water Pays Off
Water conservation has been another focus area of Tri-Star's pollutionprevention efforts that goes beyond regulated materials.
When Tri-Star expanded their fabrication business to add assembly operations, they considered the different types of systems they could use to clean flux residue from the wave solder unit. They looked into the options available in vapor degreasing or semi-aqueous cleaning. With further investigation, however, they discovered that hot deionized (DI) water could clean the boards just as effectively as the chemical-based cleaning systems. Then Tri-Star went one step further and purchased a closed-loop DI water generation system that delivers 5 to 7 gallons per minute (gpm). The system both generates DI water and recycles it through the cleaning process in a closed-loop system.
One problem Tri-Star initially experienced with the system was that solder paste was degrading the system's resin columns. In normal production this is not an issue; however, when a board requires rework, the operator runs it through the closed-loop cleaning system to remove the solder paste before reapplication. To avoid this problem, Tri-Star installed a sink on the side cleaning unit where the operator could manually clean the reject boards with the hot DI water instead of placing them on the system conveyor. The effluent from the sink is plumbed through a filter and directly to waste treatment. With this simple installation, the solder mask from the rejected boards never enters the closed-loop system, extending the life of the system's resin columns.
Because this closed-loop system was installed for a new operation, benefits compared to other technologies could not be quantified. Compared to other flux residue cleaning systems, the qualitative benefits are that it:
In another water conservation project, Tri-Star installed flow controls on rinses, increased counterflow rinsing, and implemented other "smart rinsing" techniques on their electroless copper line. By re-counting rinse water from one set of counterflow rinse tanks to another, Tri-Star cut the incoming water sources from seven to four, and reduced their water usage on the line from 19 gpm to 4 gpm, as shown in the chart below.
Although Tri-Star made these changes on the deposition line, these water use reduction ideas may be applied to other processes that use multiple rinses. To make these changes in any process, cross contamination issues must be carefully considered. To design the rinse water reuse for this line, Tri-Star set up criteria, flagging the following as "Do not contaminate" items: Do not contaminate:
copper bath with palladium from the catalyst
catalyst with cleaner/conditioner
accelerator with electroless copper
electroless copper with microetch or acids
microetch with cleaner/conditioner
In addition to water savings, these changes also reduced the amount of chemicals needed to maintain the process baths. With the "smart rinsing" water rinse set-up, the chemistry is eventually dragged back into the tank from which it was dragged out (i.e., rinse water flows back and becomes the rinse of the previous step). This has reduced the chemicals needed for additions by 25% for the affected baths (glass etch, microetch, sulfuric acid dip, and accelerator).
Overall, Tri-Star estimates that "smart rinsing" has reduced their water usage by 2.5 million gallons per year, resulting in cost savings of approximately $15,000. This is based on operating the electroless copper line for 12 to 16 hours per day, 5 days per week. The combined water and sewer fees in their area are $4.69/100 ft3 (or $6.26/1,000 gal). Additionally, they saved on chemical purchases resulting from reduced chemical use.
What is the Design for the Environment (DfE) Printed Wiring Board Project?
Representatives of the printed wiring board industry and other stakeholders entered into a partnership with the U.S. Environmental Protection Agency (EPA), called the Design for the Environment (DfE) Printed Wiring Board Project. This project is a cooperative, non-regulatory effort in which EPA, industry, and other interested parties are working together to develop technical information on pollution prevention technologies specific to the PWB industry. This information includes comparative data on the risk, performance, and cost of alternative manufacturing options.
To date, the DfE Project has focused on conducting a comprehensive evaluation of alternative technologies for making through-holes conductive. The Project is also beginning to evaluate alternatives to the hot-air-solder-leveling process. By publishing the results of these evaluations, DfE is able to provide PWB manufacturers with the information they need to make informed business decisions that take human health and environmental risk into consideration, in addition to performance and cost. The Project is also identifying and publicizing other pollution prevention opportunities in the industry through the development of PWB case studies, like this one.
EPA's Design for the Environment Program would like to thank Power Circuits for participating in this case study, and DfE PWB Project participants from the following organizations, who provided advice and guidance: Circuit Center, Inc., Concurrent Technologies Corp., DuPont Electronic Materials, Electrotek Corp., Hadco Corp., H-R Industries, Inc., and IPC.
Additional Pollution Prevention Resources for the PWB Industry
EPA's Design for the Environment Program would like to thank Tri-Star Technologies, Inc. for participating in this case study, along with the DfE PWB Project participants from the following organization who provided advice and guidance: Circuit Center, Inc., Concurrent Technologies Corp., Hadco Corp., and the Institute for Interconnecting and Packaging Electronic Circuits. Additional Pollution Prevention Resources for the PWB Industry In addition to this case study, the DfE PWB Project has prepared other case studies that examine pollution prevention opportunities for the PWB industry. All case studies are based on the experiences and successes of facilities in implementing pollution prevention projects. The other case study topics available include:
Pollution Prevention Work Practices
On-site Etchant Regeneration
Acid Recovery and Management
A Continuous-flow System for Reusing Microetchant
| The case studies, and other documents published by the
DfE Project, are available from:
Pollution Prevention Information
The DfE Program welcomes your feedback. If you have implemented any of the ideas in this series of PWB case studies, please tell us about it by calling the DfE Program at 202-260-1678 or via email at